Flue Gas Heat Recovery Project at Zouping

Climate Mitigation

With carbon emissions allowances for coal-fired power plants becoming increasingly stringent, reducing coal consumption while maintaining stable operational performance has become a crucial priority.
In response, Zouping Power Plant launched a project to enhance boiler efficiency by installing a new low-pressure economizer between the air preheater and the electric stationary precipitator (ESP). In this system, high-temperature (145℃) flue gas flows through the economizer, reducing the temperature to 115℃, to heat up the water from 85℃ to 104℃ then before returning to the deaerator of the feedwater system of the boiler.

Location

China

Project Duration

2024 – Present

Impact on Natural Capital

• Reduced 2,242 tonnes of coal consumption per year

• Saved 30,000 tonnes water consumption per year

• Reduced 5,829 tonnes CO2e per year

Impacts​
tonnes / year
Reduction of coal consumption per year
tonnes/year
Saved water consumption
tonnes CO2e per year
Reduced CO2e per year
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